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Tuning the carburetor

I rebuilt the carb a couple of years ago, but I hadn’t really done much with it aside from setting the idle and idle mixture. Based on what the plugs looked like, and the odor in the garage after I parked it, the mixture was rich. I decided to put in smaller jets to see if I could get that solved.

This carb has a metering block with replaceable jets in the primary side, and a metering plate with a fixed hole drilled in them. I wasn’t too concerned about the secondaries, and changing that would mean buying a new metering plate, or converting the plate to a metering block with jets.

There were #69 jets in the primary, which were the ones that were in it when I bought the car.

I decided to try #67 jets, and put in new plugs while I was at it.

The new jets were an improvement, but it still smelled rich. Also, there was a bog on acceleration, probably due to the smaller jets. I put on a bigger accelerator pump cam, and switched the jets down again to #65.

That change worked out great. The acceleration was smooth, no more bog. Also the engine was running smoother overall, and the garage didn’t smell after I parked the car.

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Replacing the TH350 kickdown cable – part 2

I ordered a new kickdown rod to replace the broken one. I can’t find any sign of the rest of it, and it’s a pretty big piece that’s missing, so I can only assume it has been gone for quite a while. It’s not a very complicated piece, just a piece of wire with z-bends at the ends, but I didn’t have any wire that looked sturdy enough, so I just bought one.

Getting the rod threaded into the lever that engages the kickdown piston button inside the transmission was a bit of a challenge upside down under the car, but I got there eventually. There’s a clip/pin that the lever pivots on that needs to be pulled out so you can thread the lever onto the rod. Once that is done the pin needs to go back through the 2 holes on the bracket, and the two holes on the lever, while making sure the top end of the rod doesn’t slip out of the hole on top where the cable attaches.

Once the rod was installed, I connected the cable and verified that it worked smoothly from the carb end of the cable.

From there, I put on a new filter, and a new cork gasket. I tied the gasket on with some thread to hold it in place until I got some bolts started. I then tightened the pan bolts to the recommended 10-12 inch-lb torque. Note that is INCH-pounds, not foot-pounds. Big difference. I didn’t have an inch-lb torque wrench, so I bought one specifically for this job, since I wanted to be absolutely sure it was tightened properly so it wouldn’t leak. Otherwise, I’d have to take the transmission crossmember off again to get at all the pan bolts.

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Replacing the TH350 kickdown cable

The kickdown cable is a connection between the carb and the TH350 transmission that causes the transmission to shift into a lower gear during hard acceleration. When I bought the car, the cable was not connected, and acted as though it was stuck. I assumed the sheath had melted somewhere, and that’s why it wasn’t moving. I bought a new cable, but the attachment point at the transmission was blocked by the header, so I never got around to installing it…until now.

The plan was to disconnect the right-hand side header to get access to the transmission, install the new cable, and reinstall the header.

Luckily I had help.

Headers are notorious for being difficult to install and remove. After an hour, I had the 6 bolts removed attaching the header to the cylinder head. Another hour had the 3 rusty bolts at the collector removed. The header dropped out of the way, and I had easy access to disconnect the old kickdown cable

When I took the retaining bolt off and removed the cable, it came out easily, which was bad because it’s supposed to be connected to a wire rod inside the transmission. After examining the cable, I discovered that it wasn’t melted, but the cable end was wedged up in the cable sheath, along with a piece of the rod.

In order to replace the rod, I’d have to remove the transmission pan. The original transmission in the car was a Powerglide (2-speed), and it currently has a TH350 (3-speed). The mounting points are identical between these two transmissions, but the transmission pan extends much farther back, so the rearmost pan bolts are covered up by the transmission crossmember. In order to get to those bolts, I’d have to move the crossmember out of the way.

Thankfully, the crossmember bolts and the transmission mount bolts came out easily. I jacked up the back of the transmission a little, and the crossmember slid out of the way easily.

The next challenge was getting the pan off without making a huge mess. I started with one drain pan, and quickly decided I needed a bigger one to catch all the fluid. I ended up using a big under-bed storage bin, which worked reasonably well. My wife suggested one of those pans that goes under a washing machine, I think that’s a good plan.

Once the pan was off, I expected to find the other half of the rod, but I haven’t found it yet. Maybe it was removed or lost previously. The inside of the pan looked reasonably clean, there was a very thin layer of dark (clutch?) material on it, but not a lot, so I’m hoping that’s normal. I cleaned and painted the pan because…that’s what you do when you’ve got a part off the car and have some spray paint.

I’m going to replace the filter while I have this apart, although the old filter doesn’t look very dirty. The filter kit that I got has a rubber pan gasket but some reading shows that cork works better, so I ordered a cork one because getting to the pan bolts is a problem.

To be continued…

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Winter Project 3: Distributor

The previous owner had installed an HEI distributor.  These are great units, but the install left a lot to be desired.  As I discovered when I was first trying to get the car running reliably, the wiring was incorrect, and was not supplying a full 12V to the HEI.  This resulted in it running really poorly, it would backfire and pop at pretty much anything above 1200 RPM.

My theory is that someone installed the engine and transmission, couldn’t get it running right, and never got the car on the road with the new setup.  They parked it until we bought the car.

Once the power was sorted out, the car ran much better, but it still wasn’t great.  I bought a new module for the HEI, expecting that might be the problem.  When I opened up the distributor to install the new module, I discovered that the whole distributor was in pretty sad shape.  The weights were covered in rust, the posts and the holes were very worn, and they did not move freely.  That was causing inconsistent timing, which didn’t allow the engine to run as smoothly as it could.

After looking at what it would cost in parts to rebuild the existing distributor, I ended up just buying an entirely new Accel unit for less money.

I got the 59107 distributor, which comes complete with everything…except the coil.  Oops.  I transferred the coil over from the old distributor, and will use that until I get a new one.

The challenge with changing the distributor is that it’s a little bit of a gamble on where the timing is set before you can get the engine running so you can check it with a timing light.  It doesn’t have to be exactly on the perfect position, but it needs to be at least in the general area.

As it happened, I put the new distributor in one tooth different than the old one.  It still works fine, and I was able to set the timing properly, but the vacuum can is aimed differently than the old one.  Not a big deal though.

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Winter Project 2: Rebuild Carburetor

When I first got the car running, the carb had been through a bunch of backfires and other mistreatment, including sitting for at least 18 months outside at the previous owner’s place.  While the car ran and drove okay…it wasn’t great, and still sneezed and stalled, which at best wasn’t fun, and could be dangerous in traffic.

The Carb is a Holley list 80457, which is a generic 600cfm vacuum secondary 4bbl 4160-style with electric choke.

One of the things I was worried about was how much junk from the gas tank had gotten to the carb.  The carb has a built-in filter, but when I was first getting the car to run, I added a generic inline fuel filter to trap things before they got to the carb filter.  When I removed the carb, I cut the filter open expecting to see it mostly clogged.

Amazingly, it was spotless:

That was VERY good news, because it meant the gas tank was fairly clean, and did not need to be replaced.  It also meant that there probably wasn’t a lot of junk in the carb either.

Off the car and onto the bench.  A lot of the main body was covered in soot from all the backfiring due to the badly wired HEI conversion.

After disassembling the carb, I had to find a way to clean it.  I had originally purchased a can of carb dip, but not all of the parts would fit into the can, and it was very caustic to work with.  I tried a couple of pieces in the dip, but I wasn’t impressed with the results, especially considering having to use rubber gloves to avoid chemical burns, and having to rinse everything off thoroughly afterwards.

About this time I spotted a post online about a low price for a 10-liter ultrasonic cleaner.  Usually it runs $125-150, but someone had spotted it for sale at $55 shipped.  10L was large enough to fit the main body of the carburetor, which was very handy.

I got the cleaner, filled it up with a mixture of water and Simple Green, and set the temperature on the cleaner to about 100 degrees.  It’s not very exciting when it is running, it just makes a loud buzzing noise.  No piles of bubbles, no obvious action, just the noise.

I wasn’t sure how this was going to work, so I started out slow, using 5 minute sessions with the ultrasonic cleaner on.  After a few rounds of that, I was running it for about 20 minutes (maximum time allowed by the timer on the cleaner), and that seemed to do a good job.



I experimented with the amount of Simple Green, and ended up using about 1/4 cup of it to the 10L of hot water.  When the parts came out, I rinsed them and dried them with a towel.  Because they had been heated in the cleaner, they dried really quickly.  The result was a bunch of fairly clean parts.  It’s not magic, but it did do a nice job.  Some of the tougher parts I sprayed down with carb cleaner and brake cleaner, and scrubbed with a toothbrush.


The one part that did not clean up easily was the gaskets.  These had obviously been baked on by many many years of under-hood heat.  I soaked them and ran them through the ultrasonic cleaner for many 20 minute cycles, but they just weren’t coming off.

I didn’t want to scrape too aggressively because I didn’t want to damage the surfaces.  I had some luck with plastic paint scrapers, but that was very slow going.  None of the solvents I tried had much effect on the gaskets.

I did some research and discovered there is a gasket remover product that several of the big automobile chemical houses produce.  I ended up getting the Permatex version.

It’s about the consistency of wood glue, and the bottle has a little brush built into it so you can spread it around.  This was my first attempt, and I put a little too much on.

Again, it wasn’t magic, but it did a lot of the gaskets.  I let a couple of applications soak for a while, and using the plastic scraper, I did get the gasket remains off eventually.

Almost there:

Afterwards, I gave the parts one last ride in the ultrasonic cleaner to get rid of all the little bits of gaskets, and the remains of the gasket remover.  I put all the tiny parts in a plastic bowl and put them in the cleaner as well.  It did a nice job on them, and I didn’t lose any pieces!

Next was reassembling it with new parts.  I used a Holley TricKit which came with all of the things necessary to do a rebuild.  The instructions were pretty thin on how to put it back together, so I ended up finding a guide online at

How to Assemble a Holley Carburetor: Rebuild Guide • Muscle Car DIY

It didn’t cover every detail, but it was enough so I could figure it out.

Since everything was right out of the cleaner, all of the gasoline and solvent smell was gone, so it was the perfect project to work on while watching TV in the living room.

A few shows later:

Back on the car with a new fuel filter, and…amazingly, it started right up!

Unfortunately, I hadn’t set the rear float height very well, and there was fuel pouring out of the rear bowl vent.  I shut off the car and adjusted it down a lot to stop that.  It still needed fine-tuning, but it wasn’t dripping any more.

I remembered that setting the float height was much easier (less dangerous) if you had clear sight plugs on the bowls.  I had installed them on my Nova many years ago, and adjusting the floats was simple.  When I went looking for a set, the reviews were really poor.  People reported that they dissolved overnight, or cracked, requiring taking the carb apart to clean out the pieces.  After some more reading, it seems like E85 blends are the problem, and the ethanol attacks the plugs.  No problem, I won’t leave them in I thought.

When they arrived, I installed the clear plugs and set the front float height.  The rear was still too high, and there was not enough adjustment in the screw to make it right.  So…off with the carb again, I took off the rear bowl and bent the tab on the float to lower it some.  Reassemble, put it back on the car, closer, but still not quite there.  Off again…disassemble…tweak…reassemble, reinstall.  Checking it again, I was able to adjust it to the correct level.

Great!  Now I can put the brass plugs back in and I’m done.  In the 1 minute between shutting the car off and walking around to remove the clear plugs, the rear one cracked and the head popped off, leaving the threaded part still stuck in the bowl.  It didn’t break when I tried to take it off, in fact I didn’t touch it at all.  It was just there one minute and gone the next.

Off with the carb again, disassemble, clean out the remains of the clear sight plug, and back together again…with the brass plugs instead.  I was amazed at how quickly it had broken.  They were installed for less than 3 hours total.

Moral: if you’re using these, a) work quickly, b) only barely tighten them, and c) be prepared to disassemble the bowls to get them out.  I don’t understand why someone hasn’t come up with a different plastic formula to use for these clear sight plugs.  E85 fuel has been around for a very long time, there’s no excuse for continuing to sell these ones.

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Power steering

My last classic car had manual steering…and at the time I wished I had power steering.  Now I have power steering, and kinda wish I didn’t.

The problem is that the pump is leaking for some reason.  The fluid level was very low, so I put in almost a pint of fluid.  The next day there was a giant puddle of something under the front of the car.  You guessed it, nearly a pint of power steering fluid.

Part of the problem seems to be that the engine has a mix of 68 (short water pump) and 69 (long water pump) accessories and brackets.  For the pump, it looks like it’s a 68 bracket with some spacers and washers added to make the pulleys line up.  That’s not a great plan.

The pump is leaking from the mounting hole on the back of the reservoir. (Next to the ‘notice’ sticker.)   I’m not sure, but it looks like there’s a boss inside the reservoir, and an o-ring between it and the sheetmetal of the reservoir.  Fill it up above that, and it leaks out there.  Not a great design.

The trick now is to figure out the combination of pump and brackets that will work.