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Winter Project 3: Distributor

The previous owner had installed an HEI distributor.  These are great units, but the install left a lot to be desired.  As I discovered when I was first trying to get the car running reliably, the wiring was incorrect, and was not supplying a full 12V to the HEI.  This resulted in it running really poorly, it would backfire and pop at pretty much anything above 1200 RPM.

My theory is that someone installed the engine and transmission, couldn’t get it running right, and never got the car on the road with the new setup.  They parked it until we bought the car.

Once the power was sorted out, the car ran much better, but it still wasn’t great.  I bought a new module for the HEI, expecting that might be the problem.  When I opened up the distributor to install the new module, I discovered that the whole distributor was in pretty sad shape.  The weights were covered in rust, the posts and the holes were very worn, and they did not move freely.  That was causing inconsistent timing, which didn’t allow the engine to run as smoothly as it could.

After looking at what it would cost in parts to rebuild the existing distributor, I ended up just buying an entirely new Accel unit for less money.

I got the 59107 distributor, which comes complete with everything…except the coil.  Oops.  I transferred the coil over from the old distributor, and will use that until I get a new one.

The challenge with changing the distributor is that it’s a little bit of a gamble on where the timing is set before you can get the engine running so you can check it with a timing light.  It doesn’t have to be exactly on the perfect position, but it needs to be at least in the general area.

As it happened, I put the new distributor in one tooth different than the old one.  It still works fine, and I was able to set the timing properly, but the vacuum can is aimed differently than the old one.  Not a big deal though.

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Winter Project 2: Rebuild Carburetor

When I first got the car running, the carb had been through a bunch of backfires and other mistreatment, including sitting for at least 18 months outside at the previous owner’s place.  While the car ran and drove okay…it wasn’t great, and still sneezed and stalled, which at best wasn’t fun, and could be dangerous in traffic.

The Carb is a Holley list 80457, which is a generic 600cfm vacuum secondary 4bbl 4160-style with electric choke.

One of the things I was worried about was how much junk from the gas tank had gotten to the carb.  The carb has a built-in filter, but when I was first getting the car to run, I added a generic inline fuel filter to trap things before they got to the carb filter.  When I removed the carb, I cut the filter open expecting to see it mostly clogged.

Amazingly, it was spotless:

That was VERY good news, because it meant the gas tank was fairly clean, and did not need to be replaced.  It also meant that there probably wasn’t a lot of junk in the carb either.

Off the car and onto the bench.  A lot of the main body was covered in soot from all the backfiring due to the badly wired HEI conversion.

After disassembling the carb, I had to find a way to clean it.  I had originally purchased a can of carb dip, but not all of the parts would fit into the can, and it was very caustic to work with.  I tried a couple of pieces in the dip, but I wasn’t impressed with the results, especially considering having to use rubber gloves to avoid chemical burns, and having to rinse everything off thoroughly afterwards.

About this time I spotted a post online about a low price for a 10-liter ultrasonic cleaner.  Usually it runs $125-150, but someone had spotted it for sale at $55 shipped.  10L was large enough to fit the main body of the carburetor, which was very handy.

I got the cleaner, filled it up with a mixture of water and Simple Green, and set the temperature on the cleaner to about 100 degrees.  It’s not very exciting when it is running, it just makes a loud buzzing noise.  No piles of bubbles, no obvious action, just the noise.

I wasn’t sure how this was going to work, so I started out slow, using 5 minute sessions with the ultrasonic cleaner on.  After a few rounds of that, I was running it for about 20 minutes (maximum time allowed by the timer on the cleaner), and that seemed to do a good job.



I experimented with the amount of Simple Green, and ended up using about 1/4 cup of it to the 10L of hot water.  When the parts came out, I rinsed them and dried them with a towel.  Because they had been heated in the cleaner, they dried really quickly.  The result was a bunch of fairly clean parts.  It’s not magic, but it did do a nice job.  Some of the tougher parts I sprayed down with carb cleaner and brake cleaner, and scrubbed with a toothbrush.


The one part that did not clean up easily was the gaskets.  These had obviously been baked on by many many years of under-hood heat.  I soaked them and ran them through the ultrasonic cleaner for many 20 minute cycles, but they just weren’t coming off.

I didn’t want to scrape too aggressively because I didn’t want to damage the surfaces.  I had some luck with plastic paint scrapers, but that was very slow going.  None of the solvents I tried had much effect on the gaskets.

I did some research and discovered there is a gasket remover product that several of the big automobile chemical houses produce.  I ended up getting the Permatex version.

It’s about the consistency of wood glue, and the bottle has a little brush built into it so you can spread it around.  This was my first attempt, and I put a little too much on.

Again, it wasn’t magic, but it did a lot of the gaskets.  I let a couple of applications soak for a while, and using the plastic scraper, I did get the gasket remains off eventually.

Almost there:

Afterwards, I gave the parts one last ride in the ultrasonic cleaner to get rid of all the little bits of gaskets, and the remains of the gasket remover.  I put all the tiny parts in a plastic bowl and put them in the cleaner as well.  It did a nice job on them, and I didn’t lose any pieces!

Next was reassembling it with new parts.  I used a Holley TricKit which came with all of the things necessary to do a rebuild.  The instructions were pretty thin on how to put it back together, so I ended up finding a guide online at

How to Assemble a Holley Carburetor: Rebuild Guide • Muscle Car DIY

It didn’t cover every detail, but it was enough so I could figure it out.

Since everything was right out of the cleaner, all of the gasoline and solvent smell was gone, so it was the perfect project to work on while watching TV in the living room.

A few shows later:

Back on the car with a new fuel filter, and…amazingly, it started right up!

Unfortunately, I hadn’t set the rear float height very well, and there was fuel pouring out of the rear bowl vent.  I shut off the car and adjusted it down a lot to stop that.  It still needed fine-tuning, but it wasn’t dripping any more.

I remembered that setting the float height was much easier (less dangerous) if you had clear sight plugs on the bowls.  I had installed them on my Nova many years ago, and adjusting the floats was simple.  When I went looking for a set, the reviews were really poor.  People reported that they dissolved overnight, or cracked, requiring taking the carb apart to clean out the pieces.  After some more reading, it seems like E85 blends are the problem, and the ethanol attacks the plugs.  No problem, I won’t leave them in I thought.

When they arrived, I installed the clear plugs and set the front float height.  The rear was still too high, and there was not enough adjustment in the screw to make it right.  So…off with the carb again, I took off the rear bowl and bent the tab on the float to lower it some.  Reassemble, put it back on the car, closer, but still not quite there.  Off again…disassemble…tweak…reassemble, reinstall.  Checking it again, I was able to adjust it to the correct level.

Great!  Now I can put the brass plugs back in and I’m done.  In the 1 minute between shutting the car off and walking around to remove the clear plugs, the rear one cracked and the head popped off, leaving the threaded part still stuck in the bowl.  It didn’t break when I tried to take it off, in fact I didn’t touch it at all.  It was just there one minute and gone the next.

Off with the carb again, disassemble, clean out the remains of the clear sight plug, and back together again…with the brass plugs instead.  I was amazed at how quickly it had broken.  They were installed for less than 3 hours total.

Moral: if you’re using these, a) work quickly, b) only barely tighten them, and c) be prepared to disassemble the bowls to get them out.  I don’t understand why someone hasn’t come up with a different plastic formula to use for these clear sight plugs.  E85 fuel has been around for a very long time, there’s no excuse for continuing to sell these ones.

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Winter Project 1: Fix Coolant Leak

I had put a new water pump on just before the July show, but I rushed the job, and there was a leak between the water pump and the block on the LH side.  The leak meant that  the coolant level was dropping, and the system would not hold pressure, so the temps climbed.  The fix was to pull the water pump back off again, clean everything up, and reinstall it with new gaskets.  While the system was drained, I decided to replace the old heater core hoses also.

I’ve switched the front accessory mounting brackets over to 1969+ style, which isn’t original, but is a much better arrangement than the 67-68 setup.  The earlier setup has the alternator on the LH side supported by a long thin flat bracket.  I always thought it looked awkward and not particularly secure.  For the 1969 setup, the alternator has a much beefier bracket that attaches on the RH side.  The water pump and power steering brackets are different also for the newer setup.

The heater hoses are attached to a bracket on the alternator bracket, then they go through another bracket on the inner fender, and then over to the heater core.  I wasn’t really concerned with originality, but as it turned out, the restoration-correct hoses were actually cheaper than the generic ones, so I went with those.

I really hate working with plumbing on cars.  No matter what I do, I always seem to end up with a big puddle of something on the garage floor.  I put a tube into the radiator and siphoned out all of the coolant into a bucket.  Then I started unbolting things, and when I got to the water pump…a bunch of coolant drained out onto the floor.  I put the hose into the block and siphoned out even more coolant.  That seemed to do the trick, until I disconnected the heater hoses from the heater core, and…more coolant drained out.  <sigh>

Once I got everything disassembled, I cleaned up all the surfaces, put new gaskets and RTV on, and bolted the water pump back on.  This time I let it sit for about a week before continuing.  Partly because I wanted to make sure the RTV was absolutely completely set, and partly because I was busy with other things.

The last part of the refit was installing the new hoses and the hose brackets.  The alternator bracket is the 1969+ design, but it is a chrome aftermarket one, so I had to drill a hole in it to attach the hose bracket there.  The other hose  bracket is on the inner fender.  I bought these hose brackets new from a restoration vendor.  The fender bracket didn’t want to stay in the square hole in the inner fender.  I did some digging and found that the trick is to open the bracket, and put the clip in the hole with the bracket flush against the fender.  Then take a pair of pliers and squeeze the clip from the inside of the bracket with some pliers.  That pinches the inside together, and forces the outside of the clip to spread out and attach firmly to the fender.

After everything was reassembled, a short test drive showed no leaks, and the temperature stayed right at 180*.  A successful fix.

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Odd jobs

A couple of other things I’ve taken care of recently.

New battery…

…and some gauges, since the stock instrumentation is just idiot lights:

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Freshening Center Caps

The car came with a set of rally rims including trim rings and center caps.  As other details of the car came together, the center caps started looking a bit rough by comparison.  I’m not looking for a 100% concours restoration, I just want it to look cleaner.

First step was pulling the cap and scrubbing the loose paint and dirt off of it.  I hit it with a toothbrush and some brakleen spray, and that did a decent job.

Next step was masking it off a bit before painting

Then I hit it with some satin black paint

Then I uncovered the top and gave that a quick spray to fill in the lettering

Then I wiped the paint off of the face with a paper towel and a little brakleeen spray.  A couple of passes, and the paint was removed from the face completely.

Next step was carefully wiping the paint off of the ribs on the cap, again using a paper towel and a little solvent spray.

and…finished product:

 

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Backup lights part 2

The inner panel has one large hole that the light housing sticks through, plus two small holes for the mounting studs.  The large hole is 1-7/8” in diameter, and I didn’t have  that size, so I had to wait for that to arrive in the mail.

I made a wooden template from a 2×4 to locate pilot holes for the three.  I goofed on the orientation of the holes on the RH side and didn’t realize it until the first test fit with the lamp.  Oh well…two extra holes.



I had to grind the big hole and enlarge the stud holes a bit to get the lamps to fit properly,

a quick spray to seal up the bare metal, and on to final assembly.

A little touch up and… just need to hook up the wiring.

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Console Installation Finale

I managed  to get the console installed finally…

There was a bit of last minute drama when the dashboard ashtray did not fit correctly, and the screws for the bracket are much much MUCH easier to get to with the console out, so I decided to spent a little time on that.

Somehow the previous owner had managed to screw up the opening so it was rounded on the sides.  I am still puzzled about why this was done.  I could believe the radio hole getting cut out to a larger rectangle, but that section of the dash is intact.  Why (and how?) they rounded the sides of the ashtray opening I will never understand.

I took the face plate off of the dash, and poked at it a bit, enough to get the bracket to aim the ashtray low enough to actually seat into the opening.

I also did some caveman hammer-and-dolly work on the trim plate to get that sort of back into shape again.  Someday I’ll get the ashtray fitting better and I’ll spring for a new trim plate, but it’s good enough for now.

I buttoned it all back up, and…it’s passable.  I wasn’t planning on using the ashtray anyway.

With that last hurdle out of the way, a little paint, new rubber gaskets on the shift plate, and…bolted into the car at last.

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Reupholstering and reupholstering


I got the seat base edges tacked down with zipties…and then decided I didn’t like the way it was fitting.  Note the white shows on the edges on the front and sides.  Too far back on the frame.   So, I took it apart again.

The edges were not landing where they needed to, and it was crooked.  Since the center section listing wire gets attached first, you can’t shift it afterwards.

I started over by ziptieing the middle of the listing wire to the center back attachment point of the frame.  This is about 2” in from the back edge of the frame.  That leaves enough room for the cover flap to wrap around the edge about even with the inner edge of the frame

From there, I Hinged the cover back and put batting in for the center section between the listing wires.  I ziptied the center wires to the springs, then replaced them with hogrings.


Then I moved on to filling each side section and attaching them with zipties.

…and then replaced the zipties with hogrings, and attached the rear edge flap on the cover around the rear edge of the frame.




and then the moment of truth…

The seat bottom looks fine, but the seat back looks terrible.  It’s showing the white backing, and it looks wrinkled.  I’m taking it out again to redo that soon.

 

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Reupholstering the Back Seat – Part 5

Almost done…  I got the seat base mostly done tonight.  I have to do the final batting adjustments and hog ring the outer edges down, but it’s looking like a seat again.  Good progress for the evening.

I started by attaching the burlap base and attached it around the edges.

next was inserting the new listing wire into the sleeves on the cover


for the sleeves on either side of the driveshaft hump I had to clip the ends free just inside the topstitching.  I’m not sure why they are assembled this way, but it seemed like the right thing to do.

I cut these long because the original ones were done that way with a bend at the ends.

the longest piece goes from the back corner, across the front, finishing at the other back corner.

I worked on the center section first.  It’s a bit of a guess at how much batting to use but the original wasn’t padded as much here, and it has to fit underneath the seat back.  It’s also tougher to go back and redo this so I tried hard to get it right the first time.  It’s also tough to get the hof rings in olace, so the ziptie trick helps a lot here.








once it was snugged down, i added hog rings at each speing loop

Next was the sections between the center and the side.  I kept guessing at the right amount of batting.  I adjusted it a few times and snugged the cover into place with zipties each time.


and once more for the other side